Last seen: 2020-11-03 2:56 pm
This is the Cope From HowtoMechatronics.com and as You said I did Put a debug But I think it is wrong cause I am not getting any Reading at the serial...
I tried the Howtomechatronics code for the motor control but the results are not as good as expected. Take a Look:-
Actually the motors that I am using are 12V 200 RPM Motors an on the Internet I read Somewhere they are called as the Geared BO Motors. by a Buck-Boos...
I used this Code too but motors are not even responding and like no data is being transmitted at all. Take a look:-
@casey I used the code in that post and motors are still running weirdly.Take a look Is it because of the motors the I am using here ? they are bo mo...
the serial port on my car side is not working I don't know why. I have a question, does the l298n bridge draws too much current from supply cause it...
so should i have to take a screenshot of the values in the COM port of each transmitter and Receiver ?
@freddie43 so Maybe I should try to First make a code that allows me to control the motor through simple wire connections from arduino through the joy...
Sorry it took me more than one day, here I uploaded the video on the youtube so please take a look and tell me what you think the problem is :-
@spyder Yeah maybe Today I will try to Send you a Video as soon as possible
I heavily agree with this point cause it dropped me power bank 13% low while I was testing it.
Yeah You are Right maybe i really should stop here cause maybe we can't change every code in our own way. Thank you for giving me your precious time.
@pugwash No the servo responded for a little sec but it is still not receiving anything. Please take a look is still missing ? /*---- Transmitter Co...
if you like I can send a video of my car continuously running after uploading code
yes they are same as shown in the bill's video while testing the code but when i check the IN1 and IN2 pins from my multimeter it keeps showing me som...